A door panel that flew off a Boeing 737 MAX 9 jet mid-flight on Jan. 5 appeared to be missing four key bolts, according to a preliminary report from U.S. investigators that provided the first official look into how the frightening mishap took shape.
Lawmakers and the flying public have demanded answers to what caused the panel to flyoff a brand-new Alaska Airlines-operated jet, in what has turned into a full-blown safety and reputational crisis for Boeing.
"Whatever final conclusions are reached, Boeing is accountable for what happened. An event like this must not happen on an airplane that leaves our factory," Boeing CEO Dave Calhoun said in a statement. "We simply must do better for our customers and their passengers."
The U.S. Federal Aviation Administration (FAA) grounded 171 of the Boeing 737 MAX 9 planes after the incident, most operated by U.S. carriers United Airlines and Alaska Airlines, for inspections. Those planes were cleared to return to service in late January and nearly all are flying again.
The U.S. National Transportation Safety Board (NTSB) report released on Tuesday focused on how the panel - fitted into this MAX 9 model in place of an optional exit - could have detached from the plane. The plug is held down by four bolts and then secured by "stop fittings" at 12 different locations along the side of the plug and the door frame.
Representative Rick Larsen, the top Democrat on the committee overseeing the FAA, said the "failure to re-install bolts on a safety-critical component of this 737 MAX 9 aircraft is a serious error that signals larger quality control lapses that must be corrected."
The plug was manufactured by Spirit AeroSystems, a former Boeing subsidiary. The part was produced at Spirit's facilities in Malaysia and delivered to its Wichita, Kansas, facility in May 2023. It arrived at Boeing's assembly plant in Renton, Washington on Aug. 31.
The report shows the panel had to be removed at Boeing's factory before being reinstalled. The initial findings released on Tuesday include photo evidence the bolts required to hold the plug in place appeared to be missing.
The report found the panel was first removed to repair rivet damage logged by Boeing workers on Sept. 1, a day after the panel arrived in Renton.
Investigators are still trying to determine what documentation was used to authorize the opening and closing of the plug during the rivet repair.
The report raises questions about who initially installed the bolts and why the door's opening at Renton to correct the rivets was not properly documented, said U.S. aviation safety expert John Cox.
"When was the last time those bolts were installed? Did Spirit not install them and then when Boeing opened it the guys didn't realize that they didn't have the bolts? Or did Boeing not install them? That is something that I don't think we have an answer for yet."
Senator Tammy Duckworth, who chairs an aviation subcommittee, questioned the lack of paperwork about the removal or replacement of bolts.
"It is a series of problems," Duckworth said in an interview. "What is going on between the maintenance and inspection teams... Holy cow - nobody noticed?"
Discover the latest Business News, Sensex, and Nifty updates. Obtain Personal Finance insights, tax queries, and expert opinions on Moneycontrol or download the Moneycontrol App to stay updated!
Find the best of Al News in one place, specially curated for you every weekend.
Stay on top of the latest tech trends and biggest startup news.